This is just a follow up post for my aluminum foundry flask casting progress.
The first four parts of my flask cope are casted, at this stage I have to cast four more parts for the drag part. I made a video of the molten aluminum pouring process and the sand mould shake-out.
Welcome to my FlamingFurnace, backyard metal casting blog.
Hi everyone, I mainly focus on metal casting projects using recycled ♻ scrap aluminum and other accessories in the pattern creations.
Aluminum is a very versatile material and I would like to promote the awareness of aluminum recycling via different metal casting projects.
Feel free to check my YouTube channel where I provide detailed explanations, tips & tutorials for best backyard aluminum casting methods, homemade foundry equipment & of course the importance of safety when working with molten aluminum.
So remember recycle and Enjoy my blog ;-)
May 12, 2012
April 12, 2012
Electrolysis - Rust Removal Method
This post is not really related to metal casting it's just informative and interesting. I made this video showing a method of de-rusting. It is effective, cheap and every one can try this at home.
In the images below you can see the the results of this process and how efficient it is.
You can also see the electrolysis bucket that I made, I welded bolts to rebars using them as the sacrificial anodes and plywood as a base plate.
The next two images is the electrolysis de-rusting in action!
This images are the before and after using the electrolysis rust removal method.
bringing some rusty objects back to life.
This is the video I made showing how to preform the electrolysis rust removal from a-z.
Enjoy ;-)
In the images below you can see the the results of this process and how efficient it is.
You can also see the electrolysis bucket that I made, I welded bolts to rebars using them as the sacrificial anodes and plywood as a base plate.
The next two images is the electrolysis de-rusting in action!
This images are the before and after using the electrolysis rust removal method.
bringing some rusty objects back to life.
This is the video I made showing how to preform the electrolysis rust removal from a-z.
Enjoy ;-)
April 05, 2012
Casting a new foundry flask (Part II)
Yesterday I casted the second pattern of my new aluminum foundry flask. The first attempt of the sand moulding failed. I had to improve the angle/draft around the patterns handle section. After using more filler, sanding it and then finishing with a coat of varnish.
The angle filler adjustment did the job and the sand mould second attempt was very good. I used again my homemade green sand and the aluminum casting was satisfactory.
The angle filler adjustment did the job and the sand mould second attempt was very good. I used again my homemade green sand and the aluminum casting was satisfactory.
April 03, 2012
Sand casting new foundry flask (Part I)
This is a new video I made showing the sand moulding process of my future foundry flask. In the video I made you will see the first part of the aluminum flask. I have 7 more parts to cast before it's ready for use.
This casting was made using my homemade green sand. No need for very fine casting details it's just a sand box after all ;-)
This is my sketchup design:
I made two patterns for each side of the flask, so the drag part is just a mirror image of the cope. The third pattern is my FlamingFurnace plaque name and flask size.
I made it optional to make the sand mould impression with or without it.
In the next image you can a correction I made to the gating system for the sprue, riser. This small change from the gating system I have in the video will prevent porosity.
This casting was made using my homemade green sand. No need for very fine casting details it's just a sand box after all ;-)
This is my sketchup design:
I made two patterns for each side of the flask, so the drag part is just a mirror image of the cope. The third pattern is my FlamingFurnace plaque name and flask size.
I made it optional to make the sand mould impression with or without it.
In the next image you can a correction I made to the gating system for the sprue, riser. This small change from the gating system I have in the video will prevent porosity.
March 14, 2012
Green sand casting, New Jack Plane Handles
I got a vintage Stanley jack plane no5 a few years ago and the back handle was broken where the bolt supports it, I found it was uncomfortable to work with the plane. The front handle was a bit cracked but after my baby son decided to use it as a ball it took him exactly five minutes to crack it into two halves. I don't know what material these handles where made from but it looks some type of resin before the plastic age. I decided to duplicate the two handles and sand cast new handles using my aluminum foundry. I also wanted a polished handles so it would be a unique jack plane. I checked on the internet and I did see aluminum handles that where manufacture for one of the hand planes at some stage. Making the sand mould was the easy part, creating the correct bolt core and angle for the back handle was a different story ;-)
The first casting was perfect my plan was to drill the bolt hole after the casting. The front handle drilling was accurate but on the back handle I drilled the wrong angle for the bolt to fit correctly. I experimented with different core types I didn't want to make the traditional sand core. The second and third casting of the core failed but on the forth casting I decided to use a 9mm diameter metal tube, 1.5mm thick and 6mm inner core diameter. I heated the metal tube before placing it in the flask and pouring the molten aluminum. This casting was successful.
Before I made the sand mould I reconstructed the broken end of the back handle. I used a filler and varnish to prevent the sand sticking to the pattern. I also used my foundry casting green sand and it proved again to be very suitable for this type of castings. I left a wide gating system and sprue/riser well and that prevented any casting defects. After the casting was ready I cut off the sprue and riser and drilled the bolt holes.
In the next set of images you can see the unsuccessful handle castings back in the crucible for another remelting session. After the bolt holes where done I used my buffing wheel and polished the new aluminum handles.
In the next images you can see the jack plane with the new front and back aluminum handles ready for use.
27/03/2012
Today I was making a new pattern using my jack plane with the new aluminum handles first time. works great ;-)
The first casting was perfect my plan was to drill the bolt hole after the casting. The front handle drilling was accurate but on the back handle I drilled the wrong angle for the bolt to fit correctly. I experimented with different core types I didn't want to make the traditional sand core. The second and third casting of the core failed but on the forth casting I decided to use a 9mm diameter metal tube, 1.5mm thick and 6mm inner core diameter. I heated the metal tube before placing it in the flask and pouring the molten aluminum. This casting was successful.
Before I made the sand mould I reconstructed the broken end of the back handle. I used a filler and varnish to prevent the sand sticking to the pattern. I also used my foundry casting green sand and it proved again to be very suitable for this type of castings. I left a wide gating system and sprue/riser well and that prevented any casting defects. After the casting was ready I cut off the sprue and riser and drilled the bolt holes.
In the next set of images you can see the unsuccessful handle castings back in the crucible for another remelting session. After the bolt holes where done I used my buffing wheel and polished the new aluminum handles.
In the next images you can see the jack plane with the new front and back aluminum handles ready for use.
27/03/2012
Today I was making a new pattern using my jack plane with the new aluminum handles first time. works great ;-)
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